The investigation carried out by the
USAF found the root cause of the crash to be pilots error following an engine malfunction. During the takeoff roll, engine number 1 (the left outboard engine) experienced performance fluctuations which went unnoticed until after takeoff. The engine power dropped from nearly to under , causing the aircraft to pull to the left, nearly departing the runway. The investigation found that the takeoff should have been aborted but was not. Furthermore, the investigation determined that the flight crew had failed to adequately prepare for emergency actions, and the maintenance technicians failed to properly diagnose and repair the malfunctioning engine before flight. After the flight crew retracted the landing gear, they identified that the engine No.1 was malfunctioning but did not perform the
takeoff continued after engine failure procedure or follow the
engine shutdown checklist, nor did they complete the
after takeoff checklist. The
flaps had been set to 50% for takeoff and were not retracted. The approved method of maneuvering a multi engine aircraft in such a situation is to
bank the aircraft so that the malfunctioning engine is on the high-side wing. In this case, the pilot incorrectly applied both left bank and rudder, instead of banking to the right. At an airspeed of , these incorrect inputs ultimately led to a left wing
stall resulting in a total loss of control. The maximum
altitude was at , which was insufficient to regain control of the aircraft. ==See also==