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Alaska Airlines Flight 1866

Alaska Airlines Flight 1866 was a regularly scheduled passenger flight operated by Alaska Airlines from Anchorage, Alaska, to Seattle, Washington, with several intermediate stops in southeast Alaska. The aircraft was a Boeing 727-100 with U.S. registry N2969G manufactured in 1966. On September 4, 1971, the aircraft operating the flight crashed into a mountain in Haines Borough, about 18 miles west of Juneau, Alaska, while on approach for landing. All 111 people aboard were killed. The subsequent investigation found that erroneous navigation readouts led the crew to descend prematurely. No definitive cause for the misleading data was found. It was the first fatal jet aircraft crash involving Alaska Airlines, and remained the deadliest single-aircraft accident in United States history until June 24, 1975, when Eastern Air Lines Flight 66 crashed. It is still, however, the worst air disaster in Alaska state history.

Flight crew
The captain of the flight was Richard C. Adams, age 41. Adams had 13,870 flight hours, including 2,688 hours on the Boeing 727. Piloting the aircraft at the time of the accident was First Officer Leonard D. Beach, age 32. Beach had 5,000 flight hours, with 2,100 of them on the Boeing 727. James J. Carson, age 30, was the Second Officer and had 2,850 flight hours, including about 2,600 hours on the Boeing 727. Beach and Carson were both hired by Alaska Airlines in 1966, and Adams had been with the airline since 1955. The National Transportation Safety Board (NTSB) later determined that all three flight crew members were current and qualified to operate the flight, and there was no evidence of any conditions which would have adversely affected the performance of their duties. == Aircraft ==
Aircraft
in April 1971 The aircraft was a Boeing 727-100 with U.S. registry N2969G manufactured in 1966 as c/n 19304 (line number 287). It was initially operated by Pacific Air Lines, which later became part of Hughes Airwest. On April 8, 1970, ownership of the aircraft was transferred to Hughes. Shortly thereafter, on September 25, 1970, Hughes leased it to Alaska Airlines. It had accumulated 11,344 flight hours at the time of the accident. The aircraft was powered by three Pratt & Whitney JT8D-7B turbofan engines. The NTSB determined that the aircraft and engines were properly maintained and in good working order at the time of the accident. == Accident flight ==
Accident flight
On September 4, 1971, Alaska Airlines Flight 1866 (Air Traffic Control call sign "Alaska 66") was scheduled to depart Anchorage, Alaska (ANC), with intermediate stops in Cordova (CDV), Yakutat (YAK), Juneau (JNU), and Sitka, Alaska (SIT) before continuing to Seattle, Washington (SEA). The flight departed ANC on time at 9:13 a.m. and the first stop at CDV was uneventful, apart from a minor issue with a cargo door which caused a short delay. The aircraft departed CDV at 10:34 and landed at YAK at 11:07. The next leg of the route to JNU, the accident flight, departed YAK at 11:35 a.m. with 104 passengers and 7 crew aboard. Two witnesses in the area of the Chilkat Mountains stated that they heard a low-flying jet aircraft, but could not see it because of clouds and low visibility, which they estimated at . They described the sound of the engines as normal. A short time later they heard an explosion. A third witness in the area saw a low flying plane disappear into the clouds, but did not report hearing any sound. == Investigation ==
Investigation
The U.S. NTSB investigated the accident. The cockpit voice recorder (CVR) and flight data recorder (FDR) were recovered from the crash site and read out. The wreckage was inspected, and pertinent items were removed for further study by both the NTSB and the various manufacturers. After determining that there were no apparent issues with the crew's qualifications or the aircraft, their investigation focused on the navigational equipment and techniques used for the approach. Both navigation radio receivers on the aircraft were found to be in good working order, and all ground-based navigation stations were likewise operating properly. From the CVR recording it was determined that the crew did not use the audio identification features of the navigation radios. Further, they did not use all available navigational aids to help determine their position, though it is noted that the approach they were performing did not specifically require the use of those facilities. In addition the NTSB found there was potentially a lack of crew coordination between the two pilots in their navigation radio tuning procedures. Based on the crew's conversation and the flight's erroneous position report over BARLOW intersection, the NTSB noted that the captain's navigation radio had apparently presented the crew with consistently false information at several points along the approach path. No reason for the false indications could be determined. The NTSB also found that ATC had used proper procedures in handling Flight 1866. The small aircraft that entered the airspace during their descent might have been a distraction for both the controller and the pilots. The NTSB Final Report was released on October 11, 1972. The investigation found that the following factors contributed to the accident: == Notes ==
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