Immediately after the accident,
New Scientist commented presciently on the normal official response to such events, but hoped that the opportunity would be taken to introduce effective government regulation of hazardous process plants. The Secretary of State for Employment set up a Court of Inquiry to establish the causes and circumstances of the disaster and identify any immediate lessons to be learned, and an expert committee to identify major hazard sites and advise on appropriate measures of control for them. The inquiry, chaired by
Roger Parker QC, sat for 70 days in the period September 1974 – February 1975, and took evidence from over 170 witnesses. In parallel, an Advisory Committee on Major Hazards was set up to look at the longer-term issues associated with hazardous process plants.
Circumstances of the disaster The report of the court of inquiry was critical of the installation of the bypass pipework on a number of counts: although plant and senior management were
chartered engineers (mostly chemical engineers), the post of Works Engineer which had been occupied by a chartered mechanical engineer had been vacant since January 1974, and at the time of the accident there were no professionally qualified engineers in the works engineering department. Nypro had recognised this to be a weakness and identified a senior mechanical engineer in an NCB subsidiary as available to provide advice and support if requested. At a meeting of plant and engineering managers to discuss the failure of reactor 5, the external mechanical engineer was not present. The emphasis was upon prompt restart and – the inquiry felt – although this did not lead to the deliberate acceptance of hazards, it led to the adoption of a course of action whose hazards (and indeed engineering practicalities) were not adequately considered or understood. The major problem was thought to be getting reactor 5 moved out of the way. Only the plant engineer was concerned about restarting before the reason for the failure was understood, and the other reactors inspected. The difference in elevation between reactor 4 outlet and reactor 6 inlet was not recognised at the meeting. At a working level the offset was accommodated by a dog-leg in the bypass assembly; a section sloping downwards inserted between (and joined with by mitre welds) two horizontal lengths of 20-inch pipe abutting the existing 28-inch stubs. This bypass was supported by scaffolding fitted with supports provided to prevent the bellows having to take the weight of the pipework between them, but with no provision against other loadings. The Inquiry noted on the design of the assembly: The Inquiry noted further that "there was no overall control or planning of the design, construction, testing or fitting of the assembly nor was any check made that the operations had been properly carried out". After the assembly was fitted, the plant was tested for leak-tightness by pressurising with nitrogen to 9 kg/cm2; i.e. roughly operating pressure, but below the pressure at which the system relief valve would lift and below the 30% above design pressure called for by the relevant British Standard.
Cause of the disaster The claim argued by experts retained by Nypro and their insurers was that the disaster's cause was that the 20-inch bypass was not what would have been produced or accepted by a more considered process. Controversy developed (and became acrimonious) as to whether its failure was the initiating fault in the disaster (the 20-inch hypothesis, argued by the plant designers (DSM) and the plant constructors; and favoured by the court's technical advisers), or had been triggered by an external explosion resulting from a previous failure of an 8-inch line.
The 20-inch hypothesis Tests on replica bypass assemblies showed that deformation of the bellows could occur at pressures below the safety valve setting, but that this deformation did not lead to a leak (either from damage to the bellows or from damage to the pipe at the mitre welds) until well above the safety valve setting. However theoretical modelling suggested that the expansion of the bellows as a result of this would lead to a significant amount of work being done on them by the reactor contents, and there would be considerable shock loading on the bellows when they reached the end of their travel. If the bellows were 'stiff' (resistant to deformation), the shock loading could cause the bellows to tear at pressures below the safety valve setting; it was not impossible that this could occur at pressures experienced during start-up, when pressure was less tightly controlled. (Plant pressures at the time of the accident were unknown since all relevant instruments and records had been destroyed, and all relevant operators killed). The Inquiry concluded that this ("the 20-inch hypothesis") was 'a probability' but one 'which would readily be displaced if some greater probability' could be found.
The 8-inch hypothesis Detailed analysis suggested that the 8-inch pipe had failed due to creep damage, with the formation of microscopic cavities/voids within the microstructure at a high temperature while the pipe was under pressure. The metal of the pipe would have experienced hard-to-detect deformation, microscopic cracks, and structural weakness as a result, increasing the likelihood of failure. Failure had been accelerated by contact with molten zinc; this molten zinc originating from previous small fires where zinc from galvanised steel beams and platforms had dripped on stainless steel piping; there were indications that an elbow in the pipe had been at significantly higher temperature than the rest of the pipe. The hot elbow led to a non-return valve held between two pipe flanges by twelve bolts. After the disaster, two of the twelve bolts were found to be loose; the inquiry concluded that they were probably loose before the disaster. Nypro argued that the bolts had been loose, there had consequently been a slow leak of process fluid onto lagging leading eventually to a lagging fire, which had worsened the leak to the point where a flame had played undetected upon the elbow, burnt away its lagging and exposed the line to molten zinc, the line then failing with a bulk release of process fluid which extinguished the original fire, but subsequently ignited giving a small explosion which had caused failure of the bypass, a second larger release and a larger explosion. Tests failed to produce a lagging fire with leaked process fluid at process temperatures; one advocate of the 8-inch hypothesis then argued instead that there had been a gasket failure giving a leak with sufficient velocity to induce static charges whose discharge had then ignited the leak.
The inquiry conclusion The 8-inch hypothesis was claimed to be supported by eyewitness accounts and by the apparently anomalous position of some debris post-disaster. The inquiry report took the view that explosions frequently throw debris in unexpected directions and eyewitnesses often have confused recollections. The inquiry identified difficulties at various stages of the accident development in the 8-inch hypothesis, their cumulative effect being considered to be such that the report concluded that overall the 20-inch hypothesis involving 'a single event of low probability' was more credible than the 8-inch hypothesis depending upon 'a succession of events, most of which are improbable'.
Lessons to be learned The inquiry report identified 'lessons to be learned' which it presented under various headings; 'General observation' (relating to cultural issues underlying the disaster), 'specific lessons' (directly relevant to the disaster, but of general applicability) are reported below; there were also 'general' and 'miscellaneous lessons' of less relevance to the disaster. The report also commented on matters to be covered by the Advisory Committee on Major Hazards.
General observation • Plant – where possible – should be designed so that failure does not lead to disaster on a timescale too short to permit corrective action. • Plant should be designed and run to minimise the rate at which critical management decisions arise (particularly those in which production and safety conflict). • Feedback within the management structure should ensure that top management understand the responsibilities of individuals and can ensure that their workload, capacity and competence allow them to effectively deal with those responsibilities
Specific lessons The disaster was caused by 'a well designed and constructed plant' undergoing a modification that destroyed its mechanical integrity. • Modifications should be designed, constructed, tested and maintained to the same standards as the original plant When the bypass was installed, there was no works engineer in post and company senior personnel (all chemical engineers) were incapable of recognising the existence of a simple engineering problem, let alone solving it • When an important post is vacant, special care should be taken when decisions have to be taken which would normally be taken by or on the advice of the holder of the vacant post • All engineers should learn at least the elements of branches of engineering other than their own
Matters to be referred to the Advisory Committee No one concerned in the design or construction of the plant envisaged the possibility of a major disaster happening instantaneously. It was now apparent that such a possibility exists where large amounts of potentially explosive material are processed or stored. It was 'of the greatest importance that plants at which there is a risk of instant as opposed to escalating disaster be identified. Once identified measures should be taken both to prevent such a disaster so far as is possible and to minimise its consequences should it occur despite all precautions.' There should be coordination between planning authorities and the
Health and Safety Executive, so that planning authorities could be advised on safety issues before granting planning permission; similarly the emergency services should have information to draw up a disaster plan.
Conclusion The inquiry summarised its findings as follows: ==Response to Inquiry Report==