; vital buildings were protected using water-filled perimeter "flood berms" On June 6, 2011 the Omaha Public Power District, as required by Nuclear Regulatory Commission guidelines, declared a Notification of Unusual Event (minimal level on a
4 level taxonomy) due to flooding of the Missouri River. The Missouri River was above flood stage and expected to rise further, and to remain above flood stage for several weeks to a month. Contractors installed sandbags and earthen berms to protect the facility from flooding. It was reported on June 17, 2011 that the plant was in "safe cold shutdown" mode for refueling and the anticipation of flooding, and that four weeks' worth of additional fuel had been brought in to power backup generators, should they be needed. The
Army Corps of Engineers indicated that with average precipitation, the Missouri River would not go above above sea level and OPPD officials stated that the current flood protection efforts would protect the plant to feet above sea level. Officials indicated the spent fuel pool is at above sea level. On June 7, 2011, an electrical component in a switch gear room caused a small fire with Halon extinguisher activation which forced a partial evacuation. The fire was no longer burning when the on site fire brigade arrived and according to officials, the public was never in any danger. The fire impacted pumping of coolant water through the spent fuel pool. Cooling was interrupted for an hour and a half while the estimated time for the pool to reach boiling temperature was over 88 hours. In response, the Omaha Public Power District declared an alert (second level on a
4 level taxonomy). The evacuation was the first at the facility since 1992, when (ca. 76
t) of coolant leaked into a containment building from the reactor. On June 23 a helicopter contracted by OPPD to survey transmission lines made an unplanned landing south of the plant. Reports described it as an unplanned landing although photographs showed it on its side in a field. Nobody was injured. The
Federal Aviation Administration had declared a "temporary flight restriction," in a radius, centered on the Fort Calhoun nuclear facility. This restriction went into effect on June 6, 2011, at 4:31 PM, and remains in effect "until further notice." Officials noted that the June 6 FAA directive was actually a reminder to a standing order creating no flight zones over all U.S. nuclear power plants which had been in effect after the 2001
9/11 attacks. On June 26, at 1:30 a.m., an high, long water filled rubber "flood berm" that surrounded portions of the plant was punctured by a small earth mover ("
Bobcat") and collapsed. The collapse of the flood berm allowed flood waters to surround the auxiliary and containment buildings at the plant, and also forced the temporary transfer of power from the external electricity grid to backup electrical generators. It was reported more than of water rushed in around buildings and electrical transformers. Backup generators were then used to ensure the facility maintained electrical power for cooling. The rupturing of the flood berm also resulted in approximately of petroleum being released into the river as many fuel containers were washed out. The fuel/oil containers were staged around the facility to supply fuel for pumps which remove water within the flood containment barriers. The rubber berm was a secondary measure not mandated by the NRC and was put in place by OPPD to provide additional room for work immediately outside the reactor buildings. On July 11 OPPD installed a new inflatable berm as a replacement. According to OPPD, the plant is designed to withstand waters up to above mean sea level. The river was not expected to exceed . NRC officials were at the plant at the time and NRC statements said the plant remains safe. NRC Chairman
Gregory Jaczko confirmed the plant's safety when he visited the plant on June 27. On June 30 one of the pumps used to remove seepage caught fire when a worker was refilling it with gasoline. The worker put the fire out with a fire extinguisher but was burned on his arms and face and he was airlifted via helicopter to Lincoln, Nebraska. OPPD said the fire was in an auxiliary security building area and not in the reactor area and that the plant was never in danger.
Restart Before restarting OPPD spent $180 million recommissioning the plant, and cleared a list of 450 corrective items issued by the NRC. The utility company raised rates twice whilst the plant was down, 5.9 percent in 2012 and 6.9 percent in 2013, citing these costs among other things. The newer problems discovered in 2012 inspection were not included in the calculations. After three years in cold shutdown, the plant regained full power again on December 26, 2013. Two weeks later on January 9, 2014, the plant had to stop producing power again after workers discovered a damaged
sluice gate. == Post-flood inspections ==