The ARE was operated successfully. It became
critical with a mass of
uranium-235. It was very stable as a result of its strong negative
fuel temperature coefficient (measured at -9.8e-5 dk/k/°F). The assembly was first sufficiently assembled on August 1, 1954, at which point a three-shift operation commenced for tests. Hot sodium metal was flowed through the system beginning on September 26 to test the process equipment and instrumentation. Problems with the sodium vent and sodium purification systems required lengthy repairs. After several sodium dumps and recharges, carrier salt was introduced to the system on October 25. Fuel was first added to the reactor on October 30. Initial criticality was reached at 3:45 p.m. on November 3, after a painstaking and careful process of adding the
enriched fuel. Much of the four days was spent removing plugs and repairing leaks in the enrichment line. A series of fuel samples were taken periodically. Most notably, they showed an increase in
chromium content at a rate of 50 ppm/day, indicating rapid corrosion of the fuel pipes. A series of experiments were performed in the ARE supporting its mission. • Critical experiment • Subcritical measurement of reactor temperature coefficient • Power determination at 1 watt (nominal) • Regulating rod calibration vs. fuel addition • Fuel system characteristics • Power determination at 10 watts • Regulating rod calibration vs. reactor period • Calibration of shim rod vs. regulating rod • Effect of fuel flow on reactivity • Low-power measurement of reactor temperature coefficient • Adjustment of chamber position • Approach to power: 10-kW run • Test of off-gas system • Approach to power: 100-kW to 1-MW runs • High-power measurement of the fuel temperature coefficient • High-power measurement of the reactor temperature coefficient • Reactor startup on temperature coefficient • Sodium temperature coefficient • Effect of a
dollar of reactivity • High-power measurement of reactor temperature coefficient • Moderator temperature coefficient • Xenon run at full power • Reactivity effects of sodium flow • Xenon buildup at one-tenth full power • Operation at maximum power At 4:19 p.m. on November 8, during the ascent to high power, the reactor was shut down following high airborne radioactivity measurements in the basement. It appeared that the gas fittings to the main fuel pump were leaking
fission-product gases and vapors into the pits, and the pits were leaking into the basement through defective seals in some electrical junction panels. A pipeline was run from the pits south into an uninhabited valley. Portable compressors and a jet were used to bring the pits to sub-atmospheric pressure for the rest of the experiment. The safety radiation detectors shut down the reactor a few times during restart and were withdrawn to be further away from the reactor. Eventually, the reactor started back up and reached high power. On November 12, operation of the reactor was demonstrated to Air Force and ANP personnel who had gathered at ORNL for a quarterly information meeting.
Load following was demonstrated by turning the blowers on and off. With all operational objectives attained, the decision to cease operation was made. Colonel Clyde D. Gasser was visiting the lab at this time and was invited to officiate the termination of the experiment. At 8:04 p.m., he scrammed the reactor for the last time. Much information was published about the operation of the reactor, including detailed experimental logs, power traces, and 33 lessons learned. == Decommissioning ==