The accident was investigated by the Indonesian NTSC, which was assisted by expert groups from the US, Singapore, and Australia. Around 73% of the wreckage (by weight) was recovered, partially reconstructed, and examined. Both of the aircraft recorders, the CVR and the FDR, were retrieved from the river and their data were extracted and analyzed. The investigators tested 20 different simulations for various equipment-failure scenarios, and found that the only scenario that matched the actual radar trajectory of the descent and crash of the flight was a high-speed steep dive commanded by one of the pilots. Furthermore, the investigators had found the trim jackscrew for the horizontal stabilizer, which revealed that flight inputs from one of the pilots had moved the stabilizer from level flight to a full nose-down descent. The American NTSB, which also participated in the investigation, concluded that the evidence was consistent with a deliberate manipulation of the flight controls, most likely by the captain. In a letter to the NTSC dated 11 December 2000, the NTSB wrote: Geoffrey Thomas of
The Sydney Morning Herald said, "a secret report confirmed that the Indonesian authorities would not issue a public verdict because they feared it would make their own people too frightened to fly." Santoso Sayogo, an NTSC investigator who worked on the SilkAir 185 case, said that the Indonesian investigators submitted a report which was similar to that of the NTSB's conclusion but were overruled by their boss. (his share-trading showed trading of more than one million shares and his securities-trading privileges had been suspended 10 days before the accident due to nonpayment), Investigations later revealed that his total assets were greater than his liabilities, although his liquid assets could not cover his immediate debts; his monthly income was less than his family's monthly expenditure; and he had some outstanding credit card debts. Tsu was formerly a
Republic of Singapore Air Force pilot, and had over 20 years of flying experience in the older T/
A-4S Skyhawks, as well as the newer T/
A-4SU Super Skyhawks. His last appointment was instructor pilot of a Skyhawk squadron.
CVR and FDR deactivation The CVR and FDR stopped recording minutes before the abrupt descent, but not at the same time. On 8 September 1994,
USAir Flight 427, a 737-300, crashed near
Pittsburgh, Pennsylvania, killing 132 people.
Four more incidents occurred where a 737 rudder PCU malfunction was suspected. The
Seattle Times devoted a series of 37 articles to Boeing 737 loss-of-control malfunctions. The accident occurred in the middle of a controversy over the NTSB's role in accidents caused by the rudder control unit. During the investigation of Flight 427, the NTSB had discovered that the PCU's dual servo valve could jam, as well, and deflect the rudder in the opposite direction of the pilots' input, due to thermal shock, caused when cold PCUs are injected with hot hydraulic fluid. As a result of this finding, the FAA ordered the servo valves to be replaced and new training protocol for pilots to handle unexpected movement of flight controls to be developed. The FAA ordered an upgrade of all Boeing 737 rudder control systems by 12 November 2002. ==Aftermath==