MarketBritish Airways Flight 2276
Company Profile

British Airways Flight 2276

British Airways Flight 2276 was a scheduled international passenger flight from Las Vegas, Nevada, to London Gatwick Airport, England. On 8 September 2015, the Boeing 777 operating the flight suffered an uncontained engine failure and fire in the left (#1) GE90 engine during take-off from Las Vegas-McCarran International Airport, prompting an aborted take-off and the evacuation of all passengers and crew. All 170 people on board survived, but 20 occupants were injured.

Accident
The aircraft left Terminal 3, Gate E3, at 15:53 local time, and began its take-off from Runway 07L at 16:12 where the accident occurred. After noticing what the pilot later described as a "catastrophic failure of the engine" All 170 passengers and crew escaped. One occupant was seriously injured, and others sustained minor injuries. The aircraft had reached a speed of approximately when the decision to abort was made; The fire caused a large hole in the cargo hold and damage to the engine. The Federal Aviation Administration (FAA) indicated the fire was caused by failure of the left General Electric GE90 engine, one of two fitted on the aircraft. There was a slight left-to-right wind across the runway, causing the fire to be blown towards the fuselage; the aircraft sustained localised, but major, structural damage as a result. The aircraft was equipped with suppression systems, though the systems did not extinguish the fire. == Aircraft and crew ==
Aircraft and crew
The aircraft involved was a Boeing 777-236ER, s/n 29320, registered as G-VIIO. At the time of the accident, the aircraft was 16 years old; it had been delivered new to British Airways on 26 January 1999. The captain was 63-year-old Chris Henkey, who had been with British Airways since 1973 and received his type rating on the Boeing 777 in 1999. He had 30,000 flight hours, including 12,000 hours on the Boeing 777. but following the accident he decided that Flight 2276 would be his final flight. The first officer, 30-year-old Ian Callaghan, joined the airline in 2006, receiving his type rating on the Boeing 777 in 2011, and had 6,400 flight hours, with 3,100 hours on the Boeing 777. 45-year-old relief pilot Kevin Hillyer was also on board. He had been with British Airways since 1997 and had been type rated on the Boeing 777 since 2001. The relief pilot had 14,000 flight hours, and like captain Henkey, was also well experienced on the Boeing 777 having logged 10,000 hours on it. He was a first officer at the time of the accident. == Repair ==
Repair
in February 2016, showing the unpainted fuselage skin and engine cowlingIn December 2015, British Airways announced that a team of engineers from Boeing had assessed the aircraft and determined the damage was limited and suitable for repair. As a result, it was announced that the aircraft would be repaired and returned to service. A team from Boeing completed initial repairs in February 2016. Airworthiness tests were conducted on the aircraft on 25 February 2016 and on 26 February the aircraft made its departure from Las Vegas McCarran airport at 1:33 p.m. and was flown to Victorville, arriving at 3:06 p.m. It was repainted there and further repairs and maintenance work were performed. The aircraft was then flown to British Airways Maintenance Cardiff in Cardiff on 15 March for a routine C check. Finally, it returned to its London Gatwick base and resumed passenger service on 24 March. == Investigation ==
Investigation
The National Transportation Safety Board (NTSB), the American air accident investigative body, dispatched four investigators to the site the day after the accident. As well as FAA, Boeing and General Electric involvement, the British Air Accidents Investigation Branch had a representative and that representative appointed "British Airways and the UK Civil Aviation Authority as technical advisors". Initial NTSB findings were that an uncontained engine failure had occurred and that the "left engine and pylon, left fuselage structure and inboard left wing airplane were substantially damaged by the fire". On 6 October 2015, the NTSB issued an update stating that the accident was traced to the failure of the "stage 8–10 spool in the high-pressure compressor section...liberating fragments that breached the engine case and cowling". The NTSB released their final report 2 years and 10 months later. The cause of the accident was determined as: == See also ==
tickerdossier.comtickerdossier.substack.com