s, in August 2005 As of the second quarter of 2007, Byron Clean Energy Center scored in the "green" in every
Nuclear Regulatory Commission (NRC) inspection category but one. The NRC has four levels of inspection findings; the levels are color-coded and the colors equate with risk levels. Green inspection findings represent very low risk significance. Higher levels, from white, to yellow, to red, show increasing levels of risk. For any inspection findings greater than green, the NRC conducts follow-up inspections. Unit One scored "green" in every category, while Unit Two scored "white", a step down from "green", on the inspection of the heat removal system. The inspection covered several other significant areas, including unplanned
scrams, the alert and notification system and the emergency
AC power system. From 2001–2005, no inspections of Byron Clean Energy Center found any condition that merited a greater than "green" designation, during the same time period inspection found 71 green conditions at the Byron plant. Byron, like most U.S. nuclear plants, has been the subject of various actions by the NRC. Escalated Enforcement Actions represent one type. From 1997–2007 the Byron plant has received five such actions, two of which resulted in a total of $150,000 in fines. The NRC levied an additional $55,000 in fines in October 1997 when the plant failed technical specifications surveillance guidelines. Specifically, they violated rules that require the Emergency Core Cooling System (ECCS) pump casing and discharge piping high points be vented once every 31 days. The potential safety consequence of the violation affiliated with the second fine was considered "low." A small fire occurred at the plant on the morning of February 24, 2006. As a result of the fire the plant declared an "unusual event", the least serious of the
four categories of emergency declarations by the Nuclear Regulatory Commission. On January 30, 2012, the Byron Unit 2 was shut down and depressurized after a failed insulator in the plant's switchyard caused the loss of one phase to the plant's startup transformers. This caused low voltage conditions on the plant's emergency power buses and also for two of the reactor coolant pumps to trip which caused the plant to shut down. The trip of the plant then caused the other two reactor coolant pumps to trip (as they had been receiving power directly from the main generator) and natural circulation had to be used during the shutdown. When operators discovered the loss of the single phase, they manually tripped the breaker feeding the startup transformers, allowing the emergency diesel generators to start and restore normal voltages to the safety buses. Steam was vented from the non-radioactive, secondary side of the plant to aid in the cooling process while the turbines remained offline. A small amount of radioactive tritium was released into the local environment during the initial venting procedure, but was deemed no threat to the public by the Nuclear Regulatory Commission. A similar insulator failure occurred at Unit 1 on February 29 again affecting the unit's startup transformers. In this case the breaker feeding the transformers tripped automatically and the emergency diesel generators immediately started up to restore power to the safety buses. Additionally, all of the non-safety power generation buses transferred to the unit auxiliary transformers, which receive power from the plant's turbine generator, preventing a trip of the plant. After this second failed insulator event, Exelon took both units offline and replaced all of the insulators in the plant's switchyard. On March 10, 2026, a Hydrazine exposure accident occurred causing a mass casualty incident during an outage on reactor one. ==Surrounding population==